From: Nathan Sullivan Date: Wed, 21 Oct 2015 19:17:04 +0000 (-0500) Subject: net/phy: micrel: Add workaround for bad autoneg X-Git-Url: https://git.stricted.de/?a=commitdiff_plain;h=d2fd719bcb0e;p=GitHub%2FLineageOS%2Fandroid_kernel_motorola_exynos9610.git net/phy: micrel: Add workaround for bad autoneg Very rarely, the KSZ9031 will appear to complete autonegotiation, but will drop all traffic afterwards. When this happens, the idle error count will read 0xFF after autonegotiation completes. Reset the PHY when in that state. Signed-off-by: Nathan Sullivan Signed-off-by: David S. Miller --- diff --git a/drivers/net/phy/micrel.c b/drivers/net/phy/micrel.c index 499185eaf413..cf6312fafea5 100644 --- a/drivers/net/phy/micrel.c +++ b/drivers/net/phy/micrel.c @@ -514,6 +514,27 @@ static int ksz8873mll_read_status(struct phy_device *phydev) return 0; } +static int ksz9031_read_status(struct phy_device *phydev) +{ + int err; + int regval; + + err = genphy_read_status(phydev); + if (err) + return err; + + /* Make sure the PHY is not broken. Read idle error count, + * and reset the PHY if it is maxed out. + */ + regval = phy_read(phydev, MII_STAT1000); + if ((regval & 0xFF) == 0xFF) { + phy_init_hw(phydev); + phydev->link = 0; + } + + return 0; +} + static int ksz8873mll_config_aneg(struct phy_device *phydev) { return 0; @@ -772,7 +793,7 @@ static struct phy_driver ksphy_driver[] = { .driver_data = &ksz9021_type, .config_init = ksz9031_config_init, .config_aneg = genphy_config_aneg, - .read_status = genphy_read_status, + .read_status = ksz9031_read_status, .ack_interrupt = kszphy_ack_interrupt, .config_intr = kszphy_config_intr, .suspend = genphy_suspend,