From: Roel Kluin Date: Wed, 4 Mar 2009 08:11:42 +0000 (-0800) Subject: net: more timeouts that reach -1 X-Git-Url: https://git.stricted.de/?a=commitdiff_plain;h=858b9ced6e73a0f087294c398a1ae70a7eeed94f;p=GitHub%2Fmoto-9609%2Fandroid_kernel_motorola_exynos9610.git net: more timeouts that reach -1 with while (timeout-- > 0); timeout reaches -1 after the loop, so the tests below are off by one. also don't do an '< 0' test on an unsigned. Signed-off-by: Roel Kluin Signed-off-by: David S. Miller --- diff --git a/drivers/net/arm/ks8695net.c b/drivers/net/arm/ks8695net.c index 1cf2f949c0b4..f3a127434897 100644 --- a/drivers/net/arm/ks8695net.c +++ b/drivers/net/arm/ks8695net.c @@ -560,7 +560,7 @@ ks8695_reset(struct ks8695_priv *ksp) msleep(1); } - if (reset_timeout == 0) { + if (reset_timeout < 0) { dev_crit(ksp->dev, "Timeout waiting for DMA engines to reset\n"); /* And blithely carry on */ diff --git a/drivers/net/jme.c b/drivers/net/jme.c index 08b34051c646..a6e1a35a13cb 100644 --- a/drivers/net/jme.c +++ b/drivers/net/jme.c @@ -957,13 +957,14 @@ jme_process_receive(struct jme_adapter *jme, int limit) goto out_inc; i = atomic_read(&rxring->next_to_clean); - while (limit-- > 0) { + while (limit > 0) { rxdesc = rxring->desc; rxdesc += i; if ((rxdesc->descwb.flags & cpu_to_le16(RXWBFLAG_OWN)) || !(rxdesc->descwb.desccnt & RXWBDCNT_WBCPL)) goto out; + --limit; desccnt = rxdesc->descwb.desccnt & RXWBDCNT_DCNT; diff --git a/drivers/net/ucc_geth_mii.c b/drivers/net/ucc_geth_mii.c index 54635911305c..0ada4edd56eb 100644 --- a/drivers/net/ucc_geth_mii.c +++ b/drivers/net/ucc_geth_mii.c @@ -107,7 +107,7 @@ int uec_mdio_read(struct mii_bus *bus, int mii_id, int regnum) static int uec_mdio_reset(struct mii_bus *bus) { struct ucc_mii_mng __iomem *regs = (void __iomem *)bus->priv; - unsigned int timeout = PHY_INIT_TIMEOUT; + int timeout = PHY_INIT_TIMEOUT; mutex_lock(&bus->mdio_lock); @@ -123,7 +123,7 @@ static int uec_mdio_reset(struct mii_bus *bus) mutex_unlock(&bus->mdio_lock); - if (timeout <= 0) { + if (timeout < 0) { printk(KERN_ERR "%s: The MII Bus is stuck!\n", bus->name); return -EBUSY; }