From: Peter Hurley Date: Thu, 16 Oct 2014 17:46:38 +0000 (-0400) Subject: serial: Fix divide-by-zero fault in uart_get_divisor() X-Git-Url: https://git.stricted.de/?a=commitdiff_plain;h=547039ec502076e60034eeb79611df3433a99b7d;p=GitHub%2FLineageOS%2Fandroid_kernel_motorola_exynos9610.git serial: Fix divide-by-zero fault in uart_get_divisor() uart_get_baud_rate() will return baud == 0 if the max rate is set to the "magic" 38400 rate and the SPD_* flags are also specified. On the first iteration, if the current baud rate is higher than the max, the baud rate is clamped at the max (which in the degenerate case is 38400). On the second iteration, the now-"magic" 38400 baud rate selects the possibly higher alternate baud rate indicated by the SPD_* flag. Since only two loop iterations are performed, the loop is exited, a kernel WARNING is generated and a baud rate of 0 is returned. Reproducible with: setserial /dev/ttyS0 spd_hi base_baud 38400 Only perform the "magic" 38400 -> SPD_* baud transform on the first loop iteration, which prevents the degenerate case from recognizing the clamped baud rate as the "magic" 38400 value. Reported-by: Robert Święcki Cc: # all Signed-off-by: Peter Hurley Signed-off-by: Greg Kroah-Hartman --- diff --git a/drivers/tty/serial/serial_core.c b/drivers/tty/serial/serial_core.c index df3a8c74358e..eaeb9a02c7fe 100644 --- a/drivers/tty/serial/serial_core.c +++ b/drivers/tty/serial/serial_core.c @@ -363,7 +363,7 @@ uart_get_baud_rate(struct uart_port *port, struct ktermios *termios, * The spd_hi, spd_vhi, spd_shi, spd_warp kludge... * Die! Die! Die! */ - if (baud == 38400) + if (try == 0 && baud == 38400) baud = altbaud; /*