From: Tony Lindgren Date: Fri, 20 Jan 2017 20:22:31 +0000 (-0800) Subject: serial: 8250_omap: Fix probe and remove for PM runtime X-Git-Url: https://git.stricted.de/?a=commitdiff_plain;h=4e0f5cc65098ea32a1e77baae74215b9bd5276b1;p=GitHub%2Fmoto-9609%2Fandroid_kernel_motorola_exynos9610.git serial: 8250_omap: Fix probe and remove for PM runtime Otherwise the interconnect related code implementing PM runtime will produce these errors on a failed probe: omap_uart 48066000.serial: omap_device: omap_device_enable() called from invalid state 1 omap_uart 48066000.serial: use pm_runtime_put_sync_suspend() in driver? Note that we now also need to check for priv in omap8250_runtime_suspend() as it has not yet been registered if probe fails. And we need to use pm_runtime_put_sync() to properly idle the device like we already do in omap8250_remove(). Fixes: 61929cf0169d ("tty: serial: Add 8250-core based omap driver") Signed-off-by: Tony Lindgren Signed-off-by: Greg Kroah-Hartman --- diff --git a/drivers/tty/serial/8250/8250_omap.c b/drivers/tty/serial/8250/8250_omap.c index 68a6393d9636..e7e64913a748 100644 --- a/drivers/tty/serial/8250/8250_omap.c +++ b/drivers/tty/serial/8250/8250_omap.c @@ -1235,7 +1235,8 @@ static int omap8250_probe(struct platform_device *pdev) pm_runtime_put_autosuspend(&pdev->dev); return 0; err: - pm_runtime_put(&pdev->dev); + pm_runtime_dont_use_autosuspend(&pdev->dev); + pm_runtime_put_sync(&pdev->dev); pm_runtime_disable(&pdev->dev); return ret; } @@ -1244,6 +1245,7 @@ static int omap8250_remove(struct platform_device *pdev) { struct omap8250_priv *priv = platform_get_drvdata(pdev); + pm_runtime_dont_use_autosuspend(&pdev->dev); pm_runtime_put_sync(&pdev->dev); pm_runtime_disable(&pdev->dev); serial8250_unregister_port(priv->line); @@ -1343,6 +1345,10 @@ static int omap8250_runtime_suspend(struct device *dev) struct omap8250_priv *priv = dev_get_drvdata(dev); struct uart_8250_port *up; + /* In case runtime-pm tries this before we are setup */ + if (!priv) + return 0; + up = serial8250_get_port(priv->line); /* * When using 'no_console_suspend', the console UART must not be