From: Adam Ford Date: Sat, 27 Jan 2018 21:27:05 +0000 (-0600) Subject: ARM: dts: LogicPD SOM-LV: Fix I2C1 pinmux X-Git-Url: https://git.stricted.de/?a=commitdiff_plain;h=2b8446579c1bbde6310b3a9ed7f5c4b1147466e1;p=GitHub%2Fmoto-9609%2Fandroid_kernel_motorola_exynos9610.git ARM: dts: LogicPD SOM-LV: Fix I2C1 pinmux commit 84c7efd607e7fb6933920322086db64654f669b2 upstream. The pinmuxing was missing for I2C1 which was causing intermittent issues with the PMIC which is connected to I2C1. The bootloader did not quite configure the I2C1 either, so when running at 2.6MHz, it was generating errors at times. This correctly sets the I2C1 pinmuxing so it can operate at 2.6MHz Fixes: ab8dd3aed011 ("ARM: DTS: Add minimal Support for Logic PD DM3730 SOM-LV") Signed-off-by: Adam Ford Signed-off-by: Tony Lindgren Signed-off-by: Greg Kroah-Hartman --- diff --git a/arch/arm/boot/dts/logicpd-som-lv.dtsi b/arch/arm/boot/dts/logicpd-som-lv.dtsi index 4f2c5ec75714..e262fa9ef334 100644 --- a/arch/arm/boot/dts/logicpd-som-lv.dtsi +++ b/arch/arm/boot/dts/logicpd-som-lv.dtsi @@ -97,6 +97,8 @@ }; &i2c1 { + pinctrl-names = "default"; + pinctrl-0 = <&i2c1_pins>; clock-frequency = <2600000>; twl: twl@48 { @@ -215,7 +217,12 @@ >; }; - + i2c1_pins: pinmux_i2c1_pins { + pinctrl-single,pins = < + OMAP3_CORE1_IOPAD(0x21ba, PIN_INPUT | MUX_MODE0) /* i2c1_scl.i2c1_scl */ + OMAP3_CORE1_IOPAD(0x21bc, PIN_INPUT | MUX_MODE0) /* i2c1_sda.i2c1_sda */ + >; + }; }; &omap3_pmx_wkup {