From: Sangjung Woo Date: Wed, 11 Sep 2013 21:24:21 +0000 (-0700) Subject: drivers/rtc/rtc-max77686.c: Fix wrong register X-Git-Url: https://git.stricted.de/?a=commitdiff_plain;h=1748cbf7f7c464593232cde914f5a103181a83b5;p=GitHub%2Fmoto-9609%2Fandroid_kernel_motorola_exynos9610.git drivers/rtc/rtc-max77686.c: Fix wrong register Fix a read of the wrong register when checking whether the RTC timer has reached the alarm time. Signed-off-by: Sangjung Woo Signed-off-by: Myugnjoo Ham Reviewed-by: Jonghwa Lee Signed-off-by: Andrew Morton Signed-off-by: Linus Torvalds --- diff --git a/drivers/rtc/rtc-max77686.c b/drivers/rtc/rtc-max77686.c index 9915cb96014b..9efe118a28ba 100644 --- a/drivers/rtc/rtc-max77686.c +++ b/drivers/rtc/rtc-max77686.c @@ -240,9 +240,9 @@ static int max77686_rtc_read_alarm(struct device *dev, struct rtc_wkalrm *alrm) } alrm->pending = 0; - ret = regmap_read(info->max77686->regmap, MAX77686_REG_STATUS1, &val); + ret = regmap_read(info->max77686->regmap, MAX77686_REG_STATUS2, &val); if (ret < 0) { - dev_err(info->dev, "%s:%d fail to read status1 reg(%d)\n", + dev_err(info->dev, "%s:%d fail to read status2 reg(%d)\n", __func__, __LINE__, ret); goto out; }