The latency output showed:
# | task: -3 (uid:0 nice:0 policy:1 rt_prio:99)
The comm is missing in the "task:" and it looks like a minus 3 is
the output. The correct display should be:
# | task: migration/0-3 (uid:0 nice:0 policy:1 rt_prio:99)
The problem is that the comm is being stored in the wrong data
structure. The max_tr.data[cpu] is what stores the comm, not the
tr->data[cpu].
Before this patch the max_tr.data[cpu]->comm was zeroed and the /debug/trace
ended up showing just the '-' sign followed by the pid.
Also remove a needless initialization of max_data.
Signed-off-by: Arnaldo Carvalho de Melo <acme@redhat.com>
LKML-Reference: <
1267824230-23861-1-git-send-email-acme@infradead.org>
Signed-off-by: Steven Rostedt <rostedt@goodmis.org>
__update_max_tr(struct trace_array *tr, struct task_struct *tsk, int cpu)
{
struct trace_array_cpu *data = tr->data[cpu];
- struct trace_array_cpu *max_data = tr->data[cpu];
+ struct trace_array_cpu *max_data;
max_tr.cpu = cpu;
max_tr.time_start = data->preempt_timestamp;
max_data->critical_start = data->critical_start;
max_data->critical_end = data->critical_end;
- memcpy(data->comm, tsk->comm, TASK_COMM_LEN);
+ memcpy(max_data->comm, tsk->comm, TASK_COMM_LEN);
max_data->pid = tsk->pid;
max_data->uid = task_uid(tsk);
max_data->nice = tsk->static_prio - 20 - MAX_RT_PRIO;